QUOTE (m.t. pockets @ Jul 3 2006, 01:13 PM)
THE UN OFFICIAL OFFICIAL MT POCKETS SAGA.
I put the pefect trip together. I had Jimmy Stephens and Greg Middleton on board. Greg and Jimmy have 10 times my fishing knowledge so my job was to drive and crank. Left Richmond at 0100 and untied from the dock at 0400 with more baits and rod than you would expect on a 24 ft boat. We were ready for anything.
We ran out of back river. or should i say Black River as even with the Q beam i couldnt see squat.. Made it out to the bay and navagated the sea of crab pots. Boat ran prefectly. It only has 80 Hours on her since the new motor was put in.
We got to the tunnel between the 3rd and 4th enter the waypoint for the finger at the chart mark of 65/65 and bump the throttles up to 25knots.
about 12 miles from lines in the motor stumbled once kinda got my attention then it stumble again. That time the crew woke up. I did a quick 180 turn and put us on the reverse course. I then went to the motor box to take a look.
the bildge is filling up with water. i sisnt see from where, Albe squat in the water and underway they are still ass heavy. the bilge pump has an in line fuse it poped so i jammed a peice if riggin wire in there and she started humming.
The started motor was in the water. i got it pumped out, but the bildge pump is infront to the bottom pulley on the motor and at cruse the starter is getting wet while even though the pump is dry so we slowed. letting the water move fprward.
The 32 express albe GOT FISH heard and saw the problem and folloed us for about 6 to 10 miles back until we assure dthem that we had the water problem under controll.
Thanks guys and i hope Karma smiled on you at the fishing grounds.
I got the USCG to call Sea Tow. The Raw water pump was leaking pretty heavy. and there was not a lot I could do as i lookes like the internal seals were shot.
SO I burried the trim tabs put the bow straight down and ran the bildge pump and set a course for fisherman Island.
The motor started to over heat so we would shut it down and continue to run 9 miles due east of fisheman island i dropped anchor and waited for sea tow.
we were there about 30 to 45 min when the pretty yellow Mako woth twin 250 yamys came screaming up. Thank god for Ed. We made under toe between 16 and 20Kts. we really picked up once i remebered that the tabs were town and raised them.
any way we got handed off to capt alex of sea tow to run us to the dock.
All in all that could have been a lot worse. Calm weather and an experienced crew made of less stress than i could have been.
So i am boatless right now. I cant ge the Guy who did all the work to call me back and i have put capt fatbeard on notice.
I know that the heads have gotta be cooked and the starter is shot, and i think that i need a new raw water pump as the "new" one that is on there is "tore up from the floor up".
Thanks for all the call and help out there. I will roll up my sleeves and fix it my self. Then i know that it will be better than new.
Sorry to hear about your Mech Problems. Hope its sorted out soon. Best of luck!